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creed_az_88

What's wrong with my truck?

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So I took the turbo to cooler boot off and inspected it. It's definitely wiped out.post-256-0-28212700-1411424919_thumb.jpg

I need to replace it and none of the local parts stores carry it so the question is, who to order it from.

I also found this bolt missing from the turbo. It surprisingly just layed there where it fell out and never rattled onto the ground. It can't be good but Im not sure if it affected performance at all. All the other bolts were snug. post-256-0-74986400-1411425506_thumb.jpg

I pulled the boot on the other end of the pipe going into the cooler off and the other boot looks good although the bottom side of it obviously has oil leak from the clamps.

 

 

So I'm gonna replace the torn boot and replace the missing bolt but what else should I look at? Could that torn boot really stop the truck from moving? post-256-0-64719600-1411425795_thumb.jpg

 

 

Thanks for all the help.

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Is that your glove I'm seeing thru a hole in the sleeve? You'd have trouble starting the truck with that hole in it.

 

One part I was talking about is not the rubber boot but rather that 90* plastic elbow going into the engines alum. intake, it's in your top picture and still on the truck. They make an alum. replacement for those, $120.-- Ford, maybe NAPA has those rubber boots, they look trashed and are an inexpensive replacement. I drove for some months with the rubber sleeve leaking and you'll get a poor boost code if yours were leaking.

 

If replacing those boots doesn't fix the problem, pull that EGR valve, it's easy to get to, clean it and make sure there's no holes in the diaphragm..If that valve is dirty and sticks, truck will barely run but zero power and truck will smoke like a coal burning engine.

 

Good luck.

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If that boot is torn you're not building up pressure in the turbo. I think that's your loss of power. Replace the boot and crank it.

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Usually the EGR goes bad after the oil cooler goes bad. This will cause the white smoke and blown head gaskets. New boot and pipe my just fix the problem.

Good Luck, be sure to let us know.

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So I took the turbo to cooler boot off and inspected it. It's definitely wiped out.attachicon.gifimage.jpg

I need to replace it and none of the local parts stores carry it so the question is, who to order it from.

I also found this bolt missing from the turbo. It surprisingly just layed there where it fell out and never rattled onto the ground. It can't be good but Im not sure if it affected performance at all. All the other bolts were snug. attachicon.gifimage.jpg

I pulled the boot on the other end of the pipe going into the cooler off and the other boot looks good although the bottom side of it obviously has oil leak from the clamps.

So I'm gonna replace the torn boot and replace the missing bolt but what else should I look at? Could that torn boot really stop the truck from moving? attachicon.gifimage.jpg

Thanks for all the help.

any Ford dealer will have that tube on hand. Also replaced the bolt on the compressor housing. Or http://www.amazon.com/gp/aw/d/B00BV6XWHU/ref=mp_s_a_1_1?qid=1411431810&sr=8-1

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I'm pretty sure you can only get the boot from a ford dealer. Maybe napa has them now but when I got mine napa told me to go to ford.

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Not gonna help now but I like strictly diesel.com.

 

Give Nate a call at Strictly Diesel. https://www.strictlydiesel.com/default.aspx

 

I don't know anything about the 6.0 but I've had my 7.3 since Feb of 2000 and Nate has been around for a long time and I highly recommend him. You can also (should) join http://www.azpsg.com/forum.php

 

Sunrise Ford in SoCAL sells parts a lot less than you will get them anywhere else.

 

http://www.dieselsite.com/hosesbootsandclamps.aspx

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Sorry skimmed thru the comments. first thing I would look for is a boost/vacuum leak. Sounds like a whacky Air fuel mix that's just freaking it out. Check all the intake housing and pipes and any of the vent tunes you may have coming off the manifold. A simple small vacuum or boost leak can stop an engine and rattle. Nothing too serious but it can send shivers down someone's spine when they think it's something else and their motor just took a big one

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This guy just rebuilt the top end of my buddies 6.0l power stroke. My buddy is very happy with the work and the price quote I saw seemed very reasonable. He had a cracked head, bad egr, etc.

 

http://www.bbb.org/phoenix/business-reviews/auto-repair-and-service-diesel/diesel-dermanator-llc-in-glendale-az-1000029775/

 

I also know pro diesel does good work as well.

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So I ordered a boot from rifraf diesel and installed it. I also disconnected the batteries and reconnected them just in case the truck was still in limp mode( not sure it would help but I did it anyways.) I tried starting the truck and the batteries were dead. Weird I thought considering I just put a new alternator on last week and had the batteries tested. I jumped the truck and got it to start but it took forever to jump and when I started the truck it really took a lot for it to start. In the process the gauges all pegged out. The speedometer went to 120+ or whatever it goes to the fuel gauge showed full, the oil level gauge went to full, etc. the truck ran like crap. I did get it to get above idle when pushing the fuel pedal but not by much. The motor rattled a bit but nothing like two days ago when I first broke down. I'm really wondering if this is an electrical issue. My truck batteries started to be dead when I tried to start the truck last week so put a new alternator in last week and it seemed to fix the problem. I did however feel the alternator after I put it in while it was running and it was running very hot. After the truck started all the gauges went back to normal but the fuel gauge which went back to 1/4 of a tank. I filled the tank about 30 miles prior so It should still pretty much be full. It could be wrong or it could actually be that low. I'm at work now so I can't check the actual level but if it is that low could this be bad ejectors or a bad hpop? If I decide to have a mechanic look at it, do you have any recommendations on somebody who's honest and reasonable? Preferably in Tucson or cochise county somewhere? I appreciate all comments so far.

 

 

Creed

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